Dewater Sinking Analysis of North Anchorage Caisson for the Fourth Nanjing Yangtze River Bridge
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    Abstract:

    Combined with construction of north anchorage caisson, field pumping tests were carried out. Permeability coefficient was acquired for dewater sinking. Water yield of single well and total water inflow of caisson excavation were calculated. It is found that the measured amount of total water inflow is slightly larger than the theoretical value. Based on effective stress principle, the compression of phreatic water aquifer caused by dewater is almost negligible,and the ground settlement is mainly composed of confined water aquifer compression. The calculated settlement curve along the levee was in good agreement with the measured data.

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穆保岗,朱建民,龚维明,牛亚洲.南京长江4桥北锚碇沉井的排水下沉分析[J].土木与环境工程学报(中英文),2010,32(5):135~141

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  • Received:March 15,2010
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